吉林大学学报(地球科学版)

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人工回灌物理堵塞特征试验及渗滤经验公式推导

黄修东1,束龙仓2,崔峻岭1,童坤3,周庆鹏1   

  1. 1.青岛市水文局,山东 青岛266071;
    2.河海大学水文水资源学院,南京210098;
    3.南京水利科学研究院, 南京210029
  • 收稿日期:2014-05-01 出版日期:2014-11-26 发布日期:2014-11-26
  • 作者简介:黄修东(1979-),男,工程师,博士,主要从事水资源评价和地下水资源管理方面的研究,E-mail:xdhuang_zh03@163.com
  • 基金资助:

    水利部公益性行业科研专项项目(201201024)

Test on the Characteristic of Physical Clogging During Groundwater Artificial Recharge and Derivation of Percolation Empirical Formula

Huang Xiudong1, Shu Longcang2, Cui Junling1,Tong Kun3,Zhou Qingpeng1   

  1. 1.Qingdao Bureau of Hydrology,Qingdao266071, Shandong,China;
    2.College of Hydrology and Water Resources,Hohai University,Nanjing210098,China;
    3.Nanjing Hydraulic Research Institute, Nanjing210029, China
  • Received:2014-05-01 Online:2014-11-26 Published:2014-11-26

摘要:

人工回灌是提高水资源利用水平的重要工程措施,然而回灌过程中的堵塞问题会影响入渗效率和入渗工程的使用寿命。为了深入研究堵塞的机理,以控制堵塞问题,通过砂柱试验模拟了地下水人工回灌物理堵塞过程,通过测定含水率的变化分析了由堵塞引起的砂柱饱和-非饱和状态的转化。试验中出流速率经过了迅速增大到一峰值后快速减小,然后又缓慢变小的过程,即:仅经过72 h的回灌,砂柱的出流速率减小为2.18 m/d;72 h后砂样出流速率的减小明显放缓;192 h时,砂样出流速率为0.81 m/d,约为出流速率最大值的1/10。试验结果表明:回灌水悬浮物颗粒进入砂样空隙中引起渗透性减弱,和逐渐沉积在砂柱顶部形成的淤泥层是造成堵塞的直接原因,而淤泥层的形成是造成渗滤速率迅速下降的关键因素;淤泥层的弱透水性使砂样由上至下含水率发生了变化,导致了砂样导水率和水力梯度都降低,促使回灌渗滤速率迅速减小;回灌时间越长,淤泥层厚度越大,出流速率越小。由10组对比试验的结果,综合考虑引起雨洪渗滤系统堵塞的各种因素,建立了无砾石滤料雨洪水回灌过程计算渗滤速率变化的经验模型,拟合结果决定性系数为0.932。

关键词: 人工回灌, 雨洪水地表渗滤, 堵塞, 饱和-非饱和渗流, 出流速率, 非线性最小二乘法

Abstract:

Artificial recharge is an important engineering measure to improve the level of water resource utilization. However, the clogging in the process of injection will affect the efficiency and service life of the infiltration. In order to study the theory of the clogging and to control it, experimental sand columns were used to simulate the clogging process during groundwater artifical recharge, and the saturatedunsaturated change induced by clogging was analyzed. In the test, the outflow rate increased quickly to a peak value followed by a rapid decrease, and then decreased slowly, i.e., only after 72 h of injection, the flow rate of sand column reduced to 2.18 m/d; the outflow rate of the sample decreased slowly after 72 h; the sample outflow rate was 0.81 m/d after 192 h, about 1/10 of the maximum outflow rate. The results showed that the basic reason of clogging was the permeability reduction caused by suspended matter filling the void volume of the sand and the silt layer formatted by suspended matter deposition. The formation of the silt layer was the key reason leading to the sharp decrease of the outflow rate. After the silt layer formatted, the weak permeability of it caused the water content change of the sand from upper to lower, which lead to the decrease of both hydraulic conductivity and hydraulic gradient, as a result, the outflow rate decreased rapidly. The 10 groups contrast showed that, considering the rain flood infiltration system blocking of various factors, the experience model to calculate the infiltration rate in non-gravel filter material rain flooding injection process was constructed and the fitting results decisive coefficient is 0.932.

Key words: artificial recharge, stormwater infiltration, clogging, saturated-unsaturated seepage, outflow rate, non-linear generalized least squares

中图分类号: 

  • TV211.1
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